crash video

As promised here is a short video showing the cctv footage and photos form our recent ‘incident’.

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A quick update

The safety cage is bent so will need replacing and parts of one wing as well. It has been confirmed that the repair costs are covered by my insurance, so it just a waiting game for the parts from the USA. I will miss this summer’s flying, but hope to fly her again in about 12 weeks time (my estimate not the repairers :-) )

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Good Service

I have been very lucky with the service I have got on the Rans. I rang Crispin Speers, my insurance brokers 9am Monday, by 4pm Monday it was all sorted and arranged for the UK Rans Agents, Skycraft to collect the Rans today and take it away for repair. Skycraft were there early morning to collect the aircraft, packed it all up and off they went. If the cage is badly bent (and it is visually bent) then it could be a couple of months while they get a new cage from the USA. Still, I rather wait and get it done properly. One rear spar is bent as well when is stall/spun into the ground.

I saw the video of the ‘flight’ today from a security camera. It looked quite dramatic :-) I am hoping they can get a copy of it for me and I will put it up on the blog.

Removing the wings

Ready for loading

first bit loaded

Nearly ready to go

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Good News! She WILL fly again!

I heard today that it can be repaired within my insurance limit by the UK Rans Agent. They collect it Wednesday!  :-)   :-)

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Oh Shit!

We are both OK but the plane is probably a write off!. One brake jammed on take off and I had to fly her at stall speed to miss aircraft and crews. We missed them but unfortunately I could not hold her up too long and we went in the sea wall.

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This and That

A couple of things to note for this week with a few moans. Yesterday Rosemary and I went to a meeting at Southend Airport to discuss the Olympics fiasco where the government want to effectively ban General aviation for 2 months. It was confirmed that unless you have a transponder you will be grounded in our area. If you do have a transponder then you need to file a flight plan and stick to it. What a load of CROCK! It will eliminate nearly all microlight flying in this area. If I had my way the Olympics would be banned and the government disposed of!

On another track, I am about to give up on the Airbox FastPlan flight planning software. I use the free government sponsored planning software, Skydemon Light, to do my flight planning is it is better at showing the notams etc than the paid for Fastplan. The new Fastplan is supposed to import the GPX route files (which are produced by most planning programs), does it hell, it totally corrupts them. I am now having to plan my route on Skydemon Light and then manually enter the route again on Fastplan to program the Aware. Rather a waste of effort!

Due to fly to Aero Expo at Sywell this weekend and the forecast is outside my go/no go limits at the moment. All in all I can safely say I am not a happy bunny.

 

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I don’t believe it… good flying weather on a Saturday!

Well after a long wait, today, the winds dropped, the clouds
lifted and we had some sunshine, oh, and I was not previously booked to do
something else! WE WENT FLYING!

It was really lovely up there, mainly smooth air with some turbulence
occasionally just to keep you awake.  This was the first time Rosemary had flown for
over two months, so we kept it to a local flight of an hour. We went from Stoke
around Canterbury and back via the Isle of Sheppey. In the Medway there were 6
Thames barges and they were under sail with a fire boat in front spraying water
into the air, a great sight. We dodged a few showers and had to come down a bit
occasionally to go under the clouds, but most of the flight was about 2,500’
with very good visibility. We could see the south coast as well as all the way
to Manston.

The first approach was not good, too high and too fast, and
another aircraft very close to the edge of the runway, so I threw that one away
and went around again. The second approach and landing were good and I was
happy with them. With another shower approaching, we put Hotel Sierra away and
went and had a chat with the rest of the pilots and visitors at the club house.

We had a couple of interesting things to watch as well, the Red Arrows flew
past in the distance and we also had 3 aircraft in circuit and a Spitfire flew
through the circuit, under the aircraft in circuit! Still it was good to watch,
so we forgave him. A very pleasant day was had by us.

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Flying again… at last

It has been a while, I had hoped to get a couple of days flying in this weekend, it was not to be. Saturday and Sunday were too windy (gusting 37 knots), but today, the winds were favourable, so I got a couple of quick flights in.

We finished cleaning the visible sand from the cockpit and I took off for a couple of  circuits. The wind was  almost down the runway and not to bumpy. After a couple of landings, we checked the cockpit again and removed some more sand that had appeared. Following lunch up I went again, but this time the weather was very unstable and I was thrown around a lot. Not nice, so back to the circuit. I did a really nice ‘wheeler’ landing
on the first landing, but the second one was too fast so I was bounced back into the air, so I converted that one to a 3 pointer. The wind had got blustery now, so I called it a day. Again there was more sand in the cockpit so out that came. At the moment, after each flight I am getting about a couple of tablespoons of sand appearing each flight, I have no idea where it comes from, but it should be all out soon :-(

So only 2 quick flights but it felt good to be back in the air!

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Be careful what you wish for ! :-)

Yesterday I said I wanted to go flying, I did today for one very interesting circuit and I was glad to get down again without writing off Hotel Sierra! We again checked that all the sand that we knew about was out of the cockpit by tapping the covers until no more sand appeared. All the bearings, cables and pulleys were cleaned and the controls were once again as smooth as silk.

Time for a quick test flight, the wind had dropped to about moderate 8 mph crosswind so no problems there. I carefully warmed up Hotel Sierra and did the full and free controls check several times. I lined up in 24 and opened the throttle and away we went. At about 50’ and more than half way down the runway, the elevators locked! I could move them about a third of the normal movement but even that was tight. Using engine power to control height as much as possible I did a circuit and put her on final. In only 10 minutes the crosswind had doubled :-( and I did not have full controls. Luckily I still had full aileron and rudder controls, so again using the elevators as little as possible, I brought her in using mainly engine power to control the glide. The landing was not pretty but no damage was done.

On checking Hotel Sierra, I found another half a cup of sand had appeared which was not that much of a surprise, but it had blown onto the torsion tube where it slides through the bearing on the cage. As it was all new grease on that part, the sand just stuck to it and cause the binding. After I washed all the sand/grease off it, the bar slid smoothly again. To me this is a design fault in that the sliding part of the torsion tube has no protection on it at all. I am going to make a flexible sleeve that covers the sliding part to prevent any dirt etc contaminating it again! I am also going to do the same on the thrust bearings on the control column as well as they are also open to dirt ingress.

All in all an interesting day :-) .

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I want to FLY!

Yet another week without flying, it’s been a month since my last flight! I spent today cleaning the sand from the sand blasting out of the cockpit. I thought I had filled any holes for it to get into the cockpit, but I was wrong :-) . It has all gone well, but there is sand in the thrust bearings on the control column, so I have removed them for proper cleaning at home :-( . I hope to put them back tomorrow and maybe get a quick flight in. At the moment the winds are a bit strong and nearly always crosswind. We will see what happens tomorrow…

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Good News!

After sand blasting the powder coat off the ‘cracks’ and then dye pen testing, all has passed as OK. No Cracks found !!! Just to be safe, we also tested the other side as well.

Hotel Sierra is full of sand in the cockpit, but it did need cleaning anyway :-) Next week, we will clean out the cockpit and may even go flying!  :-)

edited to add photos 8/5/11

Crack found in the powder coating

Dye testing the weld and tube

cockpit full of sand after sandblasting

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OK to start testing

My inspector gave me the OK to remove the powder coating and get the area tested for cracks. Trouble is I cannot get down there for two weeks now… :-(

Still he is hopeful that it is just corrosion and the powder coating cracked. Fingers crossed.

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Grounded! – crack found on cage!

Typical, Easter holiday, sunshine, 4 days freedom and GROUNDED :-( .

We decided to do the 6 month check of Hotel Sierra today so that we had the rest of the weekend to fly…. wrong move! On doing a close inspection of the aircraft we found a crack in the powder coating around the left hand strut attachment bracket.

Crack found in the powder coating

Note in the photo above, the bare metal is where I scraped away some of the coating to reveal the corrosion below.

I am not sure if it is corrosion under the powder coating has caused the coating to crack or a crack in the weld and tube. The fact that the crack goes halfway across a tube makes me suspect it is just the powder coating cracked, but I cannot take the risk, if I am wrong the wing could fold up in flight.

Just waiting for my inspector to get back to me to see what we do next.

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Surprisingly smooth air today

We were due to go to the Duxford safety day today but had to pull out due to other commitments. However I did get a 40 minute flight in with Karen, another pilot at Stoke. We did not take off until early afternoon and with the sunshine and no wind to speak of we did expect plenty of thermals. It was, however, surprisingly smooth up there and a joy to fly. I took off and Karen then took over until getting close to home where I took over and landed Hotel Sierra. This was the first time Karen had been in a taildragger and she was not to keen on the raising of the tail on the takeoff run :-)

When we were in the air, she liked the Rans but it has a lot less forward visibility than the Medway SLA, so she would need cushions on the seats to get a better view. The landing was long and floaty and we used up most of the runway! There was no headwind to help us and the runway was giving off a fair bit of heat. Still watching others there, they all floated :-)

Roger turned up from Linton in the X-air he is helping to get back into the air. Unfortunately we were due to be back home so did not get a lot of time to talk to him.

Only 40 minutes flying but still a good day down the airfield.

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Old Warden

A great day today, though somewhat challenging at the end of it. We flew to Old Warden today. A really nice airfield. Basically we only had time for lunch and not a look around the Shuttleworth collection on this occasion. The weather was wall to wall sunshine along with the associated thermals at the lower levels.

On the trip back, the thermals had increased and we had fun staying below the 1500’ between Stansted and Luton. I was glad we did though as at one point a 747 came over the top of us from behind and he was probably only 500’ above us. When he turned, we really caught his jet wash!

The ‘arrival’ back at Stoke was interesting. It is the worst conditions I have ever encountered there in the 8 years I have flown from there. We radioed in as we crossed the Thames and were warned that it was ‘horrid’ close to the ground. Hearing this I set up for a long shallow descent straight in from 5 miles out. It wasn’t too bad until we got to 200’ and then all hell let loose. The stick and the rudder were going from one stop to the other at a very fast rate just to try and stay straight and slightly level. We were just going to touch down when another gust took us back up to about 8’ without any real forward motion, so we landed  with a bump. On talking about it in the club hut, it had been a very interesting afternoon with everybody having trouble, even the CFI!

A great day out and we really enjoyed it.

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No flying again this weekend

At the moment I can only fly Saturdays, so flying for the next few weeks is very hit and miss. Yesterday (Saturday) was forecast to be too windy in the morning with a cold front passing overhead about midday and then flyable afterwards. Within an hour or so the forecasters were correct. About 2pm I started fueling up and then DI’ing the aircraft (Daily preflight inspection). All was going well until I spotted a fibre washer laying in the back fuselage. That was not there last time! I continued my DI knowing I would be coming back to that washer. After the normal DI I had a good look in the back of the fuselage to see where the washer had come from and noticed another loose item, a terminal screw from an instrument. I also spotted that the transponder Ariel was getting close to a rub point on the ground plane. The loose parts were investigated and it seems they came from the old 12v socket that had previously broken up and been replaced with a better quality one, they were the right size and shape and nothing was missing off the existing intruments, so that was solved (though where they have been hiding for the last 12 months, I do not know. I am assuming my deadstick fun a couple of weeks ago brought them out of their hiding place!).

After removing any rub points for the transponder ariel, and re-doing the crimp which was not as good as I would have liked, I had lost a lot of time and it was getting too late to go flying and get back for an appointment we had that evening.

Never mind, we had a good morning down there chatting with all the others on the airfield. Better luck next weekend.

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Murky weekend

No flying last weekend, the visibility was not good enough. We got ready to fly Saturday, but driving along our side of the Thames, we could not see the Kent side! The visibility was probably legal, bit it would not have been fun, so decided not to bother to drive to the airfield :-(

It is such a shame, lovely sunny days, little wind but the visibility is horrible. Still this week is due for a shakeup in the weather so we shall see what it brings.

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First Fly-in of the Year

Hotel Sierra at Cromer

What beautiful weather Saturday was, blue skies and almost no wind. We had planned on going to Cambridge to use up a free flying voucher but the weather was so nice we decided on the longer trip to Cromer for their March Hare fly-in.

It was a bit worrying that we could hear the ship’s fog horns while we were preparing Hotel Sierra for flight but once we took off the reason became clear. There was a big fog bank in the Thames Estuary.

Fog in the Thames Estuary

Another view of the fog

The hour and forty minute flight to Cromer was great with at least 20 mile visibility and not too many thermals. We spoke to several airfields on the route as we flew over them and even had to set the transponder for Norwich!

We had two attempts at landing at Cromer, both came in very fast, they changed the runway direction just after we landed by 180 degrees! J Cromer was packed with aircraft and the poor lady in their cafe was rather overwhelmed.

Cromer, very busy

We left for the return trip and the visibility had reduced dramatically and the thermals had kicked in, so the flight back was a lot harder work.

Once back into south Essex the visibility improved dramatically. All in all a great start to the fly-in season and one of the longest flights for a long time.

Here is the video blog of the trip.

Flight time: 3:25 hours
Fuel used: 32 litres

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Stow Maries visit

Hotel Sierra at Stow Maries

We visited a new airfield for us today, Stow Maries in Essex. It is a WW1 airfield that is being brought back to life. This airfield is a lovely place with 2 grass runways. It has over 30 buildings on the site, all left over from the first world war. The volunteers have started renovating some of the buildings but it will be at least 10 years before most are done. I can highly recommend a visit there for an interesting couple of hours and a very friendly setup.

We took off in 14mph winds, but at 2000′ we were getting about 25-30mph headwinds so it took 40 minutes to do a flight that would normally take 20 minutes. The journey back was only about 18 minutes in the air. :-)

At Stow Maries, it was quite gusty and I had to do an aborted landing as I got blown sideways just before touchdown which caused an almighty bounce. The next attempt was far better although I had to keep dancing on the rudder pedals right up until she stopped due to a fickle cross-wind!

We have now proved to ourselves that last week’s engine out was fuel starvation. With 7 litres of fuel in the tanks, assuming the wings are dead level (which does not happen for very long) any descent with a nose down attitude starves the engine of fuel. I am going to have to look into re-routing the pipework similar to the way they do it on the new S7 in America.

Stow Maries - Still a lot of work to do!

This is what the buildings will look like when finished

Memorial at Stow Maries Airfield

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Engine out!

Well the day started well, but I did end up in a field on the Isle of Sheppy after the engine stopped! :-)

The weather suddenly turned for the better this afternoon and the forecast for the weekend was iffy to say the best, so I took the afternoon off work for a bit of fun. The flight started well with me doing some steep turns and playing around and above the clouds. I then dived from 3500′ to 900′ doing about the 100mph to skim the coast. This was where the engine decided it wanted to have some fun as well. Then at about 900′ just off the river bank, the engine lost power. I immediately applied full power, the engine picked up and then died! At this point I was doing about 90mph about 900′ above river and marshes… oops! I turned inland and slowed to 55 mph as this gives me the best distance for least amount of height loss, checked the fuel was on, checked I had enough fuel. I then aimed for a field that looked good, but not into wind as I thought I could make this one. I perhaps should admit here, that I have never glided Hotel Sierra as I always felt the engine likes to stop in the air at very low revs so this was my first ever glide approach! I tried re-starting the engine but no go. I was now down to about 600′ so put out a call to the airfield 15 miles away, but did not expect it to get through (and it didn’t). About 200′ off the ground I saw that the field I was going to would not do as it had a ditch down the middle, so I went for the next field across and landed almost into wind.

Hotel Sierra in a field by the Isle of Sheppy Prison

This field was VERY wet and had long grass! As I got out the water came over the top of my shoes. I checked the engine and could not see any problems, so I got in and after a short period the engine started and ran perfectly…. carb ice! Now I was fairly sure of the cause. I rang the airfield to let them know I was safe and where I was and that I was going to test the engine and then (hopefully) fly home. It was arranged that Roger and John in their Thruster would come and fly as a Shepherd in-case there were other problems.

About this time, the farmer turned up so I spoke to him about what had happened and what I was going to do. He advised that I was not to go further down the field as it was a lot WETTER! He had moved his sheep off a couple of days ago as it was so wet :-( .

I taxied to the top of the field where it was only 1″ of standing water and tested the engine for another 10 minutes and then did a full power short field take off. All was OK, all I had to do now was get back to the airfield which meant crossing water again. I took the shortest route at 2300′ so that if it went wrong again I would have more time to plan next time. No problems though so I did a straight in approach to Stoke and put Hotel Sierra to bed in the Hangar. She is very muddy and will need a good wash down this weekend!

A very muddy Rans!

 

For the aviators among you, here is a synopsis of what happened. The air was cold and moist. The water temps were nowhere near the green area. I did a long descent and the water temps dropped further. The carb heaters are powered by ‘hot’ water so they failed. Long descent, low revs…. carb ice!  From 900′ I glided over 1 mile to a suitable field!

Edited to add: From discussions on the RansClan on the internet, it is quite likely that it was not carb ice, but fuel starvation! It is possible with low fuel and a long steep straight dive, to starve the engine of fuel due to the routing of the fuel pipes over the back of the wing root! Solution, do not do long STRAIGHT steep descents (when low on fuel), do a curved descent to at least keep the fuel level above the height of the wing root on one of the wings.

 Here is the video blog

Total Flight Time 1:05 hours
Fuel Used 10 Litres

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